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Flip-Chip Technology on Organic Pin Grid Array Packages (continued) FCPGA KEY CHALLENGES
Thermal Designs
![]() Figure 7: Schematic of an active heat sink solution
![]() Figure 8: Schematic of a passive heat sink solution
High-Speed Bus Impedance Requirement The design of a fixed-impedance bus structure makes it more sensitive to the physical dimension tolerances in the manufacture of the package. The FCPGA design rules will support multiple impedance targets in the package. The bus impedance specifications call for a tolerance target of +/- 10%. Impedance is a function of dielectric layer thickness, dielectric constant, and Cu trace width. This requires rigorous tolerance control of dielectric thickness. Nonuniformity in thickness of the Cu plating will directly add variability to the thickness of the dielectric layer between two adjacent Cu layers. Since there is inherent Cu thickness variation, the control of dielectric layer thickness variation becomes even more stringent. Initial data indicated this variation would be a challenge for the FCPGA package as there was a higher dielectric thickness variance than desired, and a correspondingly variable impedance value. However, as illustrated in Figure 9, impedance (Zo) measurements taken after process improvements showed that the mean impedance stabilized. The improvement was made possible through improving the Cu thickness uniformity and by making a smoother insulator surface.
![]() Figure 9: Impedance measurements with two different dielectric thicknesses
µ-Via Reliability Issues
![]() Figure 10: Example of a delaminated via Failure analysis suggested that via delamination occurred at the interface between the electrolytic Cu and electroless Cu layers. Hot oil thermal shock tests were utilized as a quick-turn reliability monitor. The measurement of improvements in the manufacturing process were based on the shifts in the m-via resistance. Test data confirmed that two factors were the significant modulators in m-via delamination. Figure 11 shows a schematic drawing of various via structures, as well as the test data for m-via resistance shift after hot oil thermal shock. The test results clearly indicated that via resistance increased more than 50% after thermal shock for some test structures. After process fixes were implemented, no via resistance shift was seen after 400 cycles of stress!
![]() Figure 11a : Schematic of various via structures
![]() Figure 11b: Via resistance before process fix
![]() Figure 11c: Via resistance after process fix The improvement in via integrity was also verified through via "pop" tests. Three types of failure modes were observed and are shown in Figure 12. None of these failure modes appeared on FCPGA packages after the process fixes were implemented.
![]() Figure 12a: Schematic of a PTH via structure
![]() Figure 12b: Popped via failure indicating weak bonding at the two Cu layers interface on package before process fix
![]() Figure 12c: Broken via edge indicating strong Cu layer interface on package after process fix
![]() Figure 12d: Broken via plug plating indicating strong bonding at the two Cu layers interface after process fix
SMT Pin Development Table 4 : SMT pin strength attributes
Test data confirmed that the smaller pin nail heads and intentional pin misalignment had lower pin strength as measured before assembly. Legs with M mg and H mg of SnAg and SnSb legs showed comparable pin pull strength and pin shear strength with the exception of the L mg SnAg lot, which had lower pin pull and pin shear strength. Interestingly, after assembly, the SnAg lots' pin pull strength was reduced significantly. Both SnSb (A%) and SnSb (B%) lots showed no sign of pin joint strength degradation after assembly. The SnSb (B%) was selected as the POR material because SnSb (A%) required a higher reflow temperature, which was undesirable.
Low Cost Underfill Material and Process Development [7] Underfill material selection criteria included raw material cost, manufacturability, reliability and process integration performance, and supplier technical support and quality. The underfill development team also reexamined the reliability and manufacturability success criteria such as alpha particle counts and the number of voids and voiding sizes, used in previous stages of development. In developing the new underfill process, viscosity and self-fillet formation are two key epoxy material properties. Based on material data sheets provided from fourteen suppliers worldwide, a total of four different materials was chosen for further evaluation. Score cards from each of the candidates were assessed to collect technical, business support, and quality data. Based on the collected information, the POR underfill material was then selected. After the POR material was finalized, the epoxy module engineering team focused on underfill process optimization. Collaborative effort from the development team resulted in an optimized and simplified underfill flow that met the FCPGA cost targets.
![]() Figure 13: A comparison of the C4-OLGA and the FCPGA underfill processes Figure 13 illustrates the differences between the C4-OLGA and the FCPGA underfill process flows. As shown in the POR flows, the FCPGA process has one, instead of two, dispensers and a BTU, which could save on equipment expenditures. Moreover, when results were evaluated, the FCPGA also improved the yield, and it had higher UPH throughput. The simplified underfill process, together with the high performance of the underfill material, was a plus for the FCPGA program.
Flip-Chip Solder Bump Non-Wet
A root cause assessment of the center non-wet showed no correlation between the microprocessor chip's passivation oxide thickness or coplanarity, the substrate's bump oxide, flux quantity, or uniformity during the chip attach process. A cross section of the center non-wet unit's solder bump joints revealed the substrate's and chips' bumps were not adequately aligned, except for those at the middle of the die. The right and left sides of the bump joints were slightly misaligned at opposite directions. Because of these observations, a failure mechanism for center non-wet was proposed; as illustrated in Figure 14, it turned out that the lack of bump coplanarity in the substrate prevented solder joints from forming at the center region of the die. This model also explained the slight shift in the alignment of the substrate's and die's bumps near the edge of the die.
![]() Figure 14: Proposed center non-wet mechanism; excessive substrate bump coplanarity prevents solder joints from forming at the center area of the die The proposed model was validated through experimentation. From the data, we also realized that a maximum substrate bump coplanarity was required to prevent center non-wet. This has been defined in the specification for incoming packages. |